147 time
I've been piddling with the 147 ...last week I fixed the tank leak and cleaned it out good. I noticed that it surged at idle quite a bit, then I noticed quite a bit of slop in the throttle shaft.
I pulled the carb , disassembled and rebuilt it with some new parts from a kit I had , and put a bushing on the throttle shaft. I REALLY took my time getting the choke plate screws out this time so I didn't snap one like I did last time with the "O". It took about 5 min each of back and forth to get them out without damage. I noticed that the throttle linkage was loose on the throttle shaft too. I could have zapped it with the MIG (and may still if this doesn't work) but I put a blob of epoxy on it to keep it from shifting. The peening done 40 yrs ago had loosened up quite a bit. The carb shaft is steel in this one, not brass as in the old Carter on the O.
Hopefully that'll smooth out the idle some .. it was good therapy either way. I'll find out later this week!
John
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61 and 63 Originals
123 (2)
782D
106,
147, 122
102 parts
It's only original ONCE!
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